Transport Woes...

SMRT to be fined $3m for major East-West Line disruption in September 2024​

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Jun 03, 2025

SINGAPORE –Rail operator SMRT will be fined $3 million for a major six-day disruption on the East-West Line (EWL) in September 2024, said the Land Transport Authority (LTA) on June 3.

LTA said the penalty was “proportionate” to the circumstances of the incident, which crippled MRT services between Jurong East and Buona Vista stations and disrupted about one in six train trips daily.

The authority said it considered the cost SMRT had borne from repairs, as well as from providing free bus and shuttle train services at the affected stations.

Releasing the findings of its months-long investigation into the incident, LTA said degraded grease was likely to have caused a faulty part of a train’s undercarriage to fall out, which precipitated the disruption on the morning of Sept 25, 2024.

The part – called an axle box, which holds the train’s wheels to the axle, a rod connecting a pair of wheels – was dislodged near Dover station while the train was being withdrawn from service to Ulu Pandan Depot.

This caused one of the train’s 12 bogies – a structure below the train carriage – to derail.

The six-car train could continue travelling as the other 11 bogies remained on the rails. But the derailed portion of the third carriage caused extensive damage to 2.55km of track and trackside equipment, such as power cables and the third rail, which supplies power to trains.

LTA found that grease keeping the axle bearings lubricated within the axle box was likely to have been degraded. The bearings are mechanical parts that allow the smooth rotation of the wheels when the train is running.

Grease that has lost lubrication capabilities can cause increased wear and tear of the bearings and, eventually, overheating.


The axle box is held in place by chevron springs – metal plates bonded together by rubber that absorb vibrations when trains are operating.

LTA said its investigation findings suggest that the bearings had produced enough heat to ignite the rubber layers between the springs, causing them to disintegrate.

With the springs progressively falling off, the axle box was then dislodged.

The axle box and bearings were badly damaged, and the grease in the axle box had been completely burned off when these parts were later recovered. Debris from the chevron springs was also too badly damaged for tests to be done to determine any initial damage before the incident, said LTA.

“It was therefore not possible to establish a definitive root cause,” it said, adding that grease samples from other axle boxes of the affected train had also shown signs of degradation.

LTA said this sequence of events was substantiated by a monitoring tool that SMRT installed near Lavender station, which detected a temperature of 118 deg C on the affected axle box earlier that morning – higher than the typical operating temperature of up to 65 deg C.


A system error, however, meant that SMRT could not identify the train on which the axle box was mounted, leading to a staff member mistakenly believing the notification to be a false warning. There was no follow-up action.

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In a separate probe into the incident, Singapore’s Transport Safety Investigation Bureau (TSIB) said it had considered two possible scenarios.

One, that the bearings had failed first due to heat and friction generated within the axle box because of the degradation of grease.

Two, that the rubber of the chevron springs had deteriorated to a point where it could no longer serve as the train’s primary suspension. This then put stress on the bearings, which eventually failed, generating heat and friction within the axle box.

However, TSIB, a department of the Ministry of Transport, said it could not determine which scenario was more likely to have occurred, owing to the severely damaged axle box and springs.

LTA, which commissioned SGS Testing and Control Services to do an independent forensic analysis, said the company found that degraded grease was a likely cause.

“While the weakened chevron spring could not be ruled out as a possible cause, the possibility was likely low,” LTA added, noting that the high temperature of the axle box detected near Lavender suggests that the bearings had failed first.

The train in question, which is no longer in use, is a Kawasaki Heavy Industries (KHI) train.

These first-generation trains are being progressively replaced by new trains, the delivery of which was delayed by 1½ years because of the Covid-19 pandemic.

The last maintenance checks on the affected train, on July 15 and Sept 10 in 2024, did not detect any anomalies.

LTA noted that SMRT had extended the interval between overhauls for the train beyond the requirement of doing so after every 500,000km travelled. The interval was extended to 575,000km in August 2022, and to 750,000km in August 2024.

At the time of the incident, the train had logged 690,000km since its last overhaul in July 2018.

During such overhauls, the axle box, bearings and chevron springs will be replaced where needed. Fresh grease will also be reapplied on the bearings.

Had the affected train been overhauled in a more timely way, the “condition of its axle box assemblies would have been checked and any degraded grease could have been replaced earlier”, LTA noted.

At the time of the incident, 18 out of 38 KHI trains that were set to undergo overhauls had been refurbished. These 18 trains had been chosen based on their reliability, mileage and condition, SMRT said.

While the authority was aware of SMRT’s procedures to vary its overhaul intervals, there was no requirement for SMRT to notify LTA when these were done.

“As axle box failures are not common, SMRT did not undertake a detailed engineering and risk assessment on extending the axle box overhaul interval,” said the regulator.

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SMRT Trains president Lam Sheau Kai told reporters at a briefing that the operator’s overhaul regime has served it well over the last 38 years.

“What may have caught us off guard this time was the convergence of factors – delays in new train deliveries due to Covid-19, our efforts to balance and adjust overhaul schedules, and the lag in receiving critical spare parts,” he said.

The pandemic disrupted global supply chains, holding up new trains and the spare parts needed for the overhauls. It also affected SMRT’s ability to do additional overhauls after 2018, the operator said.

In black-swan events such as Covid-19, it is important that SMRT and LTA come together to reassess the circumstances collectively, Mr Lam added.

“In hindsight, we could perhaps have exercised greater caution in how we managed the transition and decommissioning of the older trains.”

LTA said it would provide “more time buffer” in future purchases of trains to mitigate against unforeseen supply chain disruptions.

There have been similar incidents of axle boxes getting dislodged in other rail systems, Mr Lam said, adding these are “extremely rare, sudden and catastrophic”.

“Even for those metros, such failures caught them off guard due to their acute nature.”


More on this topic​

What triggered the six-day East-West Line MRT disruption in 2024


Interactive: How a faulty MRT train left a trail of destruction


What SMRT, LTA did after the incident​

After the incident, SMRT withdrew all KHI trains with a mileage exceeding 500,000km to undergo overhauls of the axle boxes, before they were returned to service. This was completed in October 2024.

All 16 KHI trains that are still in service will be phased out by September.

SMRT also began tapping data analytics to detect abnormal axle box temperatures earlier. It resolved the system error with its temperature-monitoring tool, and strengthened procedures for staff to raise alerts about high temperatures in a timely manner.

It has also lowered the speed of trains being withdrawn to depots under similar scenarios to 35kmh, to limit potential damage to the tracks and trackside equipment.

LTA said the affected train had been withdrawn to Ulu Pandan Depot at about 70kmh on automatic mode – which does not require driver input – in accordance with SMRT’s protocols, as its staff were not aware that doing so could exacerbate the damage.

SMRT said that during interviews for the investigation, the driver of the affected train said he did not observe irregularities or unusual occurrences as it was being withdrawn.

SMRT is also reviewing how it approves changes to maintenance regimes.

As the owner of rail assets, LTA has beefed up its oversight of how operators manage assets, including their procedures to adjust maintenance schedules.

The authority said it will work with operators for future overhaul decisions.

Operators remain responsible for their maintenance decisions, but have to flag changes to overhaul intervals for systems that are critical to safety, LTA added.

LTA said it is also engaging independent advisers to get advice on operations and maintenance strategies, as well as reliability improvements.


The major disruption – one of the worst to hit Singapore’s MRT system – affected about

500,000 out of 2.8 million train journeys

daily from Sept 25 to 30 in 2024.


It started after the train developed a fault at about 9am while travelling eastward near Clementi station.

A burning smell was detected from the faulty train, and SMRT stopped the train at Clementi station so passengers could alight, before it was withdrawn to Ulu Pandan Depot.

The train turned around at Queenstown station and was travelling westward between Dover and Clementi stations when the axle box came off.

Train services along the affected stretch resumed on Oct 1, 2024, after extensive repair and restoration works were completed on Sept 30.
 

What triggered the six-day East-West Line MRT disruption in September 2024​

Work being done on the affected train and train track right outside Ulu Pandan Depot at around 6.30pm on Sept 25, 2024.

Work being done on the affected train and train track right outside Ulu Pandan Depot at around 6.30pm on Sept 25, 2024.

Jun 03, 2025

SINGAPORE – Degraded grease in a component of an MRT train’s undercarriage was likely to have caused the six-day disruption to services on the East-West Line in September 2024, according to investigation findings that the authorities released on June 3.

Investigations by the Land Transport Authority (LTA) and the Transport Safety Investigation Bureau (TSIB) under the Ministry of Transport found that an axle box – part of the train’s undercarriage that holds the train wheels to the axle, a rod connecting a pair of wheels – became dislodged likely because of degraded grease that led to increased wear and tear on the axle bearings.

Extreme heat was generated due to the degraded grease, burning off the rubber layers of the chevron springs that supported the axle box, which was on the third carriage of the six-carriage train.

Each train carriage has two undercarriage bogies, and each bogie holds four wheels. An axle box and two sets of chevron springs are attached to each wheel.

Chevron springs absorb shock and vibration from the train’s movement and connect the axle box to the bogie frame.

Without the support of the chevron springs, the axle box fell off the affected train near Dover station as it was returning to Ulu Pandan Depot.

This dislodgement caused the wheels on the front undercarriage of the third train car to derail.

The train then severely damaged the running rails, the third rail supplying power to the trains and trackside equipment along 2.55km of tracks on the East-West Line as it headed back to the depot.

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Here is a timeline of what happened on the morning of the incident:


6.58am: The affected train started to travel westwards from Pasir Ris station to Tuas Link station.

7.23am: A sensor on the track near Lavender station detected that one of the axle boxes on the affected train had clocked a temperature of 118 deg C, above its typical range of 30 deg C to 65 deg C. But due to system issues, SMRT staff could not identify the train that was producing excess heat. The staff also thought it was a false warning and did not take further action.

8.22am: The affected train arrived at Tuas Link station.

8.25am: The train departed Tuas Link station to travel towards Pasir Ris station. About five minutes later, operations staff reported that there was a burning smell.

8.34am: The station manager of Tuas Link station checked the track of the westbound platform and reported that there was no burning smell there.

8.50am-8.52am: The station manager of Clementi station boarded the affected train to carry out an inspection and reported that there was a burning smell inside.


8.53am: The operations control centre requested that passengers disembark the affected train
so that it can return to Ulu Pandan Depot. To return to the depot from Clementi station, the train had to travel eastwards to a crossover track located between Queenstown and Redhill stations to turn around.

9.04am: When the train arrived at Dover station, the station manager boarded the affected train to conduct checks. He reported a burning smell inside the train, but did not notice any smoke. At the same time, the train driver did not notice any signs of a train fault.

9.08am: The train turned around from the eastbound track to the westbound track near Queenstown station.

9.16am: A power trip occurred when the train was travelling westwards between Dover and Clementi stations, but it was able to move into Clementi station. The train driver and station manager of Dover station – who was still on board – did not notice any burning smell or smoke.

9.19am: Traction power was restored. The Dover station manager alighted at Clementi station and the train continued moving towards Ulu Pandan Depot.

9.20am: Another power trip happened and the affected train stalled on the track leading to Ulu Pandan Depot. The operations control centre could not restore traction power.

9.28am: The operations control centre sent a recovery team to rescue the train. They found that four wheels of the train’s front undercarriage had come off the rails, and the axle box on the third train car had fallen off near Dover station.

9.52am: SMRT alerted the public to the disruption between Boon Lay and Queenstown stations on its Facebook page.

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